1988 rebuild update
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Hello, it's as close as can be, not genuine but compares to original, had a problem starting surprisingly, ran perfectly when I remitted to frame, could hear air being drawn in,. Would run with choke but stall as soon as turned off. Somehow I must have dislodged carb from rubber boot of reed inlet between then and now, not a lot but enough for a small air leak on the inlet side. Remade and idling fine with good pickup on the throttle. Keen to try on the road as soon as I can arrange and find time for mot. Repainted exhaust stinks as well!
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Looks like it's just left the showroom bud
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Have ordered the bar ends, spare time today so thought I would check and take for mot, difficult to start again! Checked all usual suspects and thought fuel starvation to blame, could get to start on choke but running off choke poor, decided to take carb out and found inlet rubber split below jubilee clip! Ordered from cmsl as fowlers had no stock,none on eBay either! 60 odd euros including postage, not pleased. To be expected for 29 yr old rubber parts I suppose, assume it split after initial reassembly as started and ran perfectly when first reassembled. At least I found the problem, just have to wait a week or so for delivery now
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Only the ones with the additional intake silencer attachment will be left before long
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@nottsbiker said in 1988 rebuild update:
Only the ones with the additional intake silencer attachment will be left before long
Which one is that?
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Like those fitted to late DTR / DT-X etc had a hole for another yeis type bottle to plug in and act I'm guessing as an intake silencer
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@nottsbiker looked on cmsl exploded diagrams, can only see the pattern as mine even for later bikes, same part no? May seal mine with self amalgamating tape while I am waiting, (I get bored easily!)